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dow-uap-d48-report-september-1996
p178 / 146
      depletion before to reaching cutoff conditions. Impact was 28 miles short of
      target.
28.   146, 16 Dec 58, Response Mode 4, Flight Phase 1: Although flight was considered
      a success, the main-engine fuel valve remained partially open for 14 seconds after
      MECO command was given. This resulted in a 6-mile overshoot.
29.   149, 30 Dec 58, Response Mode 2, Flight Phase 1: A momentary ground in the
      electrical system at liftoff caused the guidance system to assume control at this
      time rather than the planned 108.5 seconds. Guidance immediately commanded a
      maximum pitch rate to place the missile in its proper orientation for 108.5
      seconds. ·By 22 seconds the missile has pitched through 46°. As it attempted to
      maintain stability, a reverse pitch subsequently developed, but by 46.4 seconds
      the missile was tumbling to the right. Destruct was sent at 52.5 seconds.

30.   128 (Able 11), 22 Jan 59, Response Mode 4, Flight Phase 1.5: An electrical failure
      prevented second-stage (Aerojet General AJl0-42) separation and ignition.

31.   154, 30 Jan 59, Response Mode 4, Flight Phase 1: Improper propellant mixture and
      low thrust resulted in fuel depletion before cutoff conditions were reached.
32.   131 (Able II), 28 Feb 59, Response Mode 4, Flight Phase 2: Flight appeared normal
      until 195 seconds when all track was lost. As a result, the RSO sent cutoff at 218
      seconds and destruct at 222 seconds.

44.. 194, 29 June 59, Response Mode NA, Flight Phase 1.5: Flight was normal except
     that reentry vehicle did not separate and retro rockets did not fire.
45.   203, 21 July 59, Response Mode 3, Flight Phase 1: The liftoff pin failed to extract so
      the pitch and roll programs were not initiated. Missile was destroyed at 45
      seconds at an altitude of about 18,000 feet.
52.   136 (Transit 1A), 17 Sep 59, Response Mode 4, Flight Phase 2.5: First and second
      stages performed normally until stage 2/3 separation. Failure of the stage-2 retro
      system apparently led to a collision of the stages. As a result, the third stage
      failed to ignite.
59.   254, 1 Dec 59, Response Mode 4T, Flight Phase 1: A hydraulic-system failure
      resulted in premature closure of the main-engine liquid-oxygen valve. The
      hydraulic-system pressure decayed almost linearly from 8 seconds to 146 seconds
      when missile control was lost. Impact was 322 miles short of target.
66.   257 (Transit 1B), 13 Apr 60, Response Mode NA, Flight Phase 1 and 5: The flight
      was a partial success although satellite was placed in a lower-than-planned orbit.
      MECO velocity was 315 ft/sec below normal. Noisy data rejected by the guidance
      computer resulted in pitch-plane steering errors and the unplanned orbit.


9/10/96                                     169                                         RTI


Vision Description (EN)

This is a clean, unredacted page of text containing a numbered list of flight mission summaries from 1958 to 1960. The entries describe technical details and outcomes of various flight phases, including mentions of 'Able II' and 'Transit' missions. The layout is a standard report format with a footer indicating page 169 and a date of 9/10/96.

Descrição Vision (PT-BR)

Esta é uma página de texto limpa e sem rasuras, contendo uma lista numerada de resumos de missões de voo de 1958 a 1960. As entradas descrevem detalhes técnicos e resultados de várias fases de voo, incluindo menções às missões 'Able II' e 'Transit'. O layout é um formato de relatório padrão com um rodapé indicando a página 169 e a data de 9/10/96.